WASHINGTON, D.C. -- The National Transportation Safety Board
yesterday issued the following brief o the fatal Amtrak derailment
in Nodaway, Iowa, which occurred on March 17, 2001.
Derailment of Amtrak Train No. 5-17 on Burlington Northern
and Santa Fe Railway Track near Nodaway, Iowa, March 17, 2001
Accident No.: DCA-01-MR-003
Location: Nodaway,
Iowa
Date of Accident: March 17, 2001
Time: 11:40 p.m. central
standard time
Railroads: Burlington Northern and Santa Fe Railway
National Railroad Passenger Corporation (Amtrak)
Fatalities:
1
Injuries: 77
Property Damage: $3.38 million
Type of
Accident: Derailment
The Accident
On March 17,
2001, about 11:40 p.m. central standard time, westbound Amtrak train
No. 5-17, the California Zephyr, derailed near Nodaway, Iowa. Amtrak
train No. 5-17 consisted of 2 locomotive units and 16 cars. All but
the last five cars derailed. No fire or hazardous materials were
involved in the accident. The train crew consisted of an engineer
and 2 conductors with 13 on-board service personnel. In addition,
241 passengers were on the train. As a result of the derailment, 78
people were injured, including 1 fatal injury.
Amtrak train
No. 5-17 had been operating over class 4 track belonging to the
Burlington Northern and Santa Fe Railway (BNSF)1 Creston Subdivision
at the time of the derailment. A broken rail was discovered at the
point of derailment.
The train had originated at Chicago,
Illinois, at 3:35 p.m. on March 17, 2001, (30 minutes late) and was
destined for Oakland, California. The train crew had boarded at
Chicago. The engineer on duty when the accident occurred had
relieved the original engineer at Ottumwa, Iowa, milepost (MP) 280,
about 9:00 p.m.
As the train progressed on its assigned
route, the engineer found that the horn/whistle on the lead
locomotive failed near Murray, Iowa, MP 370, around 10:21 p.m. He
advised the dispatcher for the district of the problem and discussed
the failure with the conductor. They decided that the conductor
would ride in the second locomotive and activate the horn/whistle on
the second locomotive when the train approached and passed through
grade crossings. They used this procedure until, at Corning, Iowa,
MP 414, the train entered a different train dispatcher's district.
The new train dispatcher, upon learning of the malfunctioning
horn/whistle, instructed the crew to reduce the speed of the train
at the grade crossings rather than use the horn/whistle on the
second unit. The conductor of train No. 5-17 came forward and rode
in the lead locomotive with the engineer to assist him in observing
the crossings. The engineer stated (and event recorder information
confirmed) that he began reducing the train's speed at grade
crossings. At MP 418.94, the train speed had been 16 mph while
passing through a grade crossing. The engineer was accelerating the
train during the approach to the accident site (MP 419.92). The
event recorder indicated that, at MP 419.90, the train was traveling
at 52 mph.
The engineer stated that near MP 419.90, he felt
a "tugging" sensation in connection with the train's progress and
heard a "grinding, screeching noise," so he made an emergency brake
application about 11:40 p.m. When the locomotives came to a stop,
the engineer and conductor looked back and realized that the train's
cars had uncoupled from the locomotives, and most cars had derailed.
The cars were about 1/8 mile behind the stopped locomotives. The
engineer radioed the dispatcher and asked him to contact emergency
responders. The conductor walked back and surveyed the damage. After
reaching the cars, the conductor radioed the engineer and said,
"...the wreck look[s] real bad." The conductor found the assistant
conductor, and they cared for the passengers. Soon thereafter, local
emergency medical service personnel began to arrive and immediately
started to evacuate the injured from the train. The emergency
response effort was completed by 4:00 a.m., March 18.
A
broken rail was discovered at the point of derailment. The broken
pieces of rail were reassembled at the scene, and it was determined
that they came from a 15-foot, 6-inch section of rail that had been
installed as replacement rail at this location in February 2001. The
replacement had been made because, during a routine scan of the
existing rail on February 13, 2001, the BNSF discovered internal
defects near MP 419.92. A short section of the continuous welded
rail that contained the defects was removed, and a piece of
replacement rail was inserted. This rail, referred to as a "plug,"
was used to replace the defective rail segment. The plug rail did
not receive an ultrasonic inspection before or after installation.
It would have been visually inspected for obvious surface damage,
defects, and excessive wear before installation.
The Safety
Board could not reliably determine the source of the plug rail. Two
different accounts were given concerning its origin. The local
supervisor said the rail came from his inventory of rail and had
been in the inventory for several years. Another engineering manager
thought that the rail had come from a rail rehabilitation facility
in Springfield, Missouri. In either case, the replacement rail would
have been rail removed from another track location for reuse.
Portions of the broken plug rail were sent to the National
Transportation Safety Board laboratory for further analysis. The
analysis indicated that the rail had multiple internal defects.
Specifically, the laboratory found that the rail failed due to
fatigue initiating from cracks associated with the precipitation of
internal hydrogen. Cracks associated with the precipitation of
internal hydrogen occur in steels due to excessive hydrogen content
produced during processing.
Replacing Defective Rails
At the time of the accident, the BNSF was revising the
directions for replacing defective rail that appear in its BNSF
Engineering Instructions. The revised BNSF instructions added four
new items for maintenance personnel to consider when selecting a
replacement rail.2 None of the new selection instructions would have
disqualified the Nodaway plug rail segment for use as a replacement
rail.
According to the engineering instructions, as revised
March 1, 2001, the BNSF was aware that defective rail might be
replaced with another piece of defective rail. The manual stated:
Poor quality rail used for defect removal may itself become
defective. One survey found that 17 percent of defects during the
month measured were in rails installed to remove previous
defects.
Altogether (including the four new instructions),
the BNSF Engineering Instructions list seven guidelines to help
personnel avoid using a defective rail to replace a known defective
rail. The guidelines are based on previously determined methods of
identifying marginal rail. For example, they state "Do not use `A'
rails or non-control cooled rail 112# or heavier for replacement in
main track and sidings," because historical experience has shown
that "A" rail and non-control cooled rail have a relatively high
incidence of internal defects. All seven guidelines rely on external
indicators or previous knowledge of the rail to disqualify the
replacement piece. Nothing in the instructions requires BNSF
personnel to scan replacement rail for internal defects before
installing it in place of a known defective rail.
Regulatory
Requirements
Title 49 Code of Federal Regulations (CFR)
213.113 provides guidelines for replacing defective rail. The
regulations are primarily concerned with the nature of the defect in
the rail, the circumstances under which the defective rail may
temporarily continue in use, and the timetables for replacing the
defective rail. Nothing in the regulations provides a screening
process for selecting or ensuring the quality of a replacement rail.
Title 49 CFR 213.233 provides track inspection requirements.
The required inspection periods for class 4 track are twice weekly,
with at least 1 calendar day between inspections. The BNSF exceeded
these criteria and conducted daily inspections on the section of
track where the accident took place. According to regulation,
inspections must be performed either "on foot or by riding over the
track in a vehicle at a speed that allows the person making the
inspection to visually inspect the track structure for compliance
with this part."
Title 49 CFR 213.237 requires that rail
systems conduct "A continuous search for internal defects" on their
tracks. For class 4 track, the minimum frequency of inspection
required is "at least once every 40 mgt or once a year, whichever
interval is shorter." Again, the BNSF exceeded these criteria with
respect to the accident area and scanned the rail for internal
defects once every 30 days.
Actions Taken Since the Accident
Since the Nodaway accident, the BNSF has required its
maintenance personnel to scan some replacement rails for internal
defects before the rails are inserted into existing track. However,
the testing requirement applies only to main tracks over which
passenger trains travel and/or which have train densities of at
least 20 mgt per year.3 The BNSF has approximately 29,043 miles of
main track, of which 9,157 track miles are on passenger routes, and
10,126 track miles are on nonpassenger routes that carry more than
20 mgt per year.
The Safety Board is not aware of any class
I railroad other than the BNSF with a procedure for checking the
internal quality of rail being used to replace known defective rail.
Most railroads rely on the fact that all existing rail is
ultrasonically scanned while in place on the track, in accordance
with the requirements at 49 CFR 213.237. Therefore, if a piece of
rail has been removed from a track location and stored for future
use as replacement rail, a railroad may assume that the replacement
rail was scanned while in its previous location and that it passed
that inspection. However, this was the process used for the plug
rail that failed in the Nodaway accident, and that plug rail was, in
fact, defective.
Probable Cause
The National
Transportation Safety Board determines that the probable cause of
the derailment of Amtrak train No. 5-17 was the failure of the rail
beneath the train, due to undetected internal defects. Contributing
to the accident was the Burlington Northern and Santa Fe Railway's
lack of a comprehensive method for ensuring that replacement rail is
free from internal defects.
Adopted: March 5, 2002
Recommendations
As a result of its investigation
of the Nodaway, Iowa, railroad accident, the National Transportation
Safety Board makes the following safety recommendations:
To
the Federal Railroad Administration:
Require railroads to
conduct ultrasonic or other appropriate inspections to ensure that
rail used to replace defective segments of existing rail is free
from internal defects. (R-02-5)
To Class I and Passenger
Railroads (except the Burlington Northern and Santa Fe Railway):
Conduct ultrasonic or other appropriate inspections on all
rail used to replace defective segments of existing rail to ensure
that the replacement rail is free from internal defects.
(R-02-6)
To the Burlington Northern Santa Fe Corporation:
Implement a permanent policy of inspecting for internal
defects, using ultrasonic or other appropriate means, any rail used
to replace a defective segment of existing rail. (R-02-7)